Tao Lei, Li Songyan, Cheng Shiqing. Foamed Acid Plug-Removal Technique for Horizontal Wells in Heavy Oil Reservoirs[J]. Petroleum Drilling Techniques, 2015, 43(6): 76-80. DOI: 10.11911/syztjs.201506014
Citation: Tao Lei, Li Songyan, Cheng Shiqing. Foamed Acid Plug-Removal Technique for Horizontal Wells in Heavy Oil Reservoirs[J]. Petroleum Drilling Techniques, 2015, 43(6): 76-80. DOI: 10.11911/syztjs.201506014

Foamed Acid Plug-Removal Technique for Horizontal Wells in Heavy Oil Reservoirs

More Information
  • Received Date: March 09, 2015
  • Revised Date: November 14, 2015
  • In this paper, a series of studies was conducted on the foamed acid plug-removal technique used to to remove near wellbore contaminants in horizontal wells in heavy oil reservoirs .The studies were conducted drilling and production to improve plug removal effects. Based on foam performance evaluation experiments and near wellbore contaminant corrosion tests, the formula of foamed acid system was optimized with the heavy oil reservoirs in the west of Block Zheng 411 as the examples. The sand pack core flooding experiment and foamed acid viscosity test were conducted on foamed acid to study its sand carrying and suspending capacities. The optimized formula was good in foaming properties with foaming volume of 380 mL and half-life time of 450 s. It was excellent in terms of sand carrying and suspension capacity. Its maximum viscosity was 2 629 mPa·s, and the sand settling velocity in the foamed acid could be ignored. This technique was applied in 12 wells in the west of Block Zheng 411. Thus, production cycle was extended by 71 d and the oil incremental per cycle averaged 1 080 t. It was shown that this technique could remove the near wellbore contaminants of horizontal wells in heavy oil reservoirs efficiently and greatly increase oil production.
  • [1]
    郭富凤,赵立强,刘平礼,等.水平井酸化工艺技术综述[J].断块油气田,2008,15(1):117-120. Guo Fufeng,Zhao Liqiang,Liu Pingli,et al.Overview of acidizing technology of horizontal well[J].Fault-Block Oil Gas Field,2008,15(1):117-120.
    [2]
    赵益忠,孙磉礅,高爱花,等.稠油油藏蒸汽吞吐井长效防砂技术[J].石油钻探技术,2014,42(3):90-94. Zhao Yizhong,Sun Sangdun,Gao Aihua,et al.Long-term sand control technology for multiple round steam huff and puff wells in heavy oil reservoirs[J].Petroleum Drilling Techniques,2014,42(3):90-94.
    [3]
    Cheng L,Kam S I,Delshad M,el al.Simalation of dynamic foam-acid diversion processes[R].SPE 68916,2001.
    [4]
    Alvarez J M,Rivas H,Navarro G.An optimal foam quality for diversion in matrix acidizing projects[R].SPE 58711,2000.
    [5]
    马喜平,许帅,王晓磊,等.低压气藏用低密度无固相泡沫修井液的研制及试验[J].石油钻探技术,2015,43(5):100-105. Ma Xiping,Xu Shuai,Wang Xiaolei,et al.Development and experiment of low-density and solid-free foam workover fluid for low pressure gas reservoir[J].Petroleum Drilling Techniques,2015,43(5):100-105.
    [6]
    于清艳,张烈辉,王鑫杰.高温高盐底水油藏强化泡沫体系试验研究[J].石油钻探技术,2015,43(2):97-103. Yu Qingyan,Zhang Liehui,Wang Xinjie.An experimental study of enhanced foam systems used in high temperature and high salinity bottom water reservoirs[J].Petroleum Drilling Techniques,2015,43(2):97-103.
    [7]
    舒小波,孟英峰,万里平,等.可循环强抑制性稳定泡沫钻井液研究[J].石油钻探技术,2014,42(4):69-74. Shu Xiaobo,Meng Yingfeng,Wan Liping,et al.Recyclable and highly inhibitive stable foam drilling fluid[J].Petroleum Drilling Techniques,2015,42(4):69-74.
    [8]
    徐建军.泡沫调剖改善多元热流体开采效果技术研究与应用[J].石油钻采工艺,2015,37(2):114-116. Xu Jianjun.Research and application of improving multiple thermal fluid recovery effect by profile control with foam[J].Oil Drilling Production Technology,2015,37(2):114-116.
    [9]
    李兆敏,孙茂盛,林日亿,等.泡沫封堵及选择性分流实验研究[J].石油学报,2007,28(4):115-118. Li Zhaomin,Sun Maosheng,Lin Riyi,et al.Laboratory study on foam plugging and selective divided-flow[J].Acta Petrolei Sinica,2007,28(4):115-118.
    [10]
    Nguyen Q P,Rossen W R,Zitha P L J,et al.Determination of gas trapping with foam using X-ray CT and effluent analysis[R].SPE 94764,2005.
    [11]
    李宾飞,李兆敏,徐永辉,等.泡沫酸酸化技术及其在气井酸化中的应用[J].天然气工业,2006,26(12):130-132. Li Binfei,Li Zhaomin,Xu Yonghui,et al.Foamed acid acidizing and its application on gas well[J].Natural Gas Industry,2006,26(12):130-132.
    [12]
    杨红兵.泡沫流体技术在稠油油藏中的应用[J].胜利油田职工大学学报,2008,22(5):51-53. Yang Hongbing.Application of foam fluid technology on heavy oil reservoir[J].Journal of Shengli Oilfield Staff University,2008,22(5):51-53.
    [13]
    王登庆.水平井砾石充填防砂工艺研究[D].东营:中国石油大学(华东)石油工程学院,2008. Wang Dengqing.Research on sand control technology of gravel pack of horizontal well[D].Dongying:China University of Petroleum (Huadong),School of Petroleum Engineering,2008.
    [14]
    李兆敏,王冠华,曹小朋.泡沫混排解堵技术研究与应用[J].西南石油大学学报:自然科学版,2010,32(2):178-181. Li Zhaomin,Wang Guanhua,Cao Xiaopeng,et al.Research and application of foam plug removal technology[J].Journal of Southwest Petroleum University:Science Technology Edition,2010,32(2):178-181.
    [15]
    李书光.大学物理实验[M].北京:科学出版社,2012:46-50. Li Shuguang.University physics experiments[M].Beijing:Science Press,2012:46-50.
  • Related Articles

    [1]ZHOU Peng, DU Xiaoyou, CAO Yanfeng, YU Jifei, JIANG Haiwei, XUE Qilong. Experimental Research on Permeability Enhancement and Plug Removal by Means of an Electric Explosion Shock Wave[J]. Petroleum Drilling Techniques, 2020, 48(2): 98-103. DOI: 10.11911/syztjs.2020033
    [2]LI Xinyong, LI Chunyue, ZHAO Bing, FANG Haoqing, HUANG Yanfei, HU Wenting. Acidizing Technology for Deep Penetration in Main Fault Zone of Shunbei Oil and Gas Field[J]. Petroleum Drilling Techniques, 2020, 48(2): 82-87. DOI: 10.11911/syztjs.2020014
    [3]FANG Junwei, ZHANG Yi, LI Shuanggui, YU Peizhi, LI Yinting. Acid-Soluble Temporary Plugging Technology for Ultra-Deep Fractured Carbonate Reservoirs in Block 1 of the Shunbei Area[J]. Petroleum Drilling Techniques, 2020, 48(2): 17-22. DOI: 10.11911/syztjs.2020006
    [4]LUO Wei, LIN Yongmao, DONG Haifeng, WU Qiang. Wellbore Blockage Removing Technologies in the Yuanba Gas Field[J]. Petroleum Drilling Techniques, 2018, 46(5): 109-114. DOI: 10.11911/syztjs.2018116
    [5]ZHANG Xiong, GENG Yudi, JIAO Kebo, HOU Fan, LUO Pandeng. The Technology of Multi-Stage Acid Fracturing in Horizontal Well for Carbonate Reservoir by Temporary Plugging Ways in the Tahe Oilfield[J]. Petroleum Drilling Techniques, 2016, 44(4): 82-87. DOI: 10.11911/syztjs.201604015
    [6]Li Shuang, Dong Bo, Kong Fangqing, Xie Yongbin. New Technology for Stuck Drill Pipe Using Mud Loss-Proof Emulsified Acid Implemented in a Ultra-Deep Horizontal Well in the Yuanba Gas Field[J]. Petroleum Drilling Techniques, 2015, 43(2): 44-49. DOI: 10.11911/syztjs.201502008
    [7]Zuo Weiqin, Li Xuelian, Lu Yiyu, Liu Yong. Key Parameters of Removing Blockage with Rotating Jets and Sand-Tubes[J]. Petroleum Drilling Techniques, 2014, 42(6): 92-96. DOI: 10.11911/syztjs.201406018
    [8]Mu Lijun, Zhu Hongzheng, Lü Yiming, Wang Bai, Li Dajian, Niu Caiyun. Design and Application of Water Detecting and Plugging Pipe String for Low Production Horizontal Wells[J]. Petroleum Drilling Techniques, 2014, 42(1): 91-94. DOI: 10.3969/j.issn.1001-0890.2014.01.018
    [9]Wang Yuxi. Application of Ultra-Short Radius Horizontal Well Drilling Technology in Plugging Removal in Injectors[J]. Petroleum Drilling Techniques, 2013, 41(5): 89-92. DOI: 10.3969/j.issn.1001-0890.2013.05.017
  • Cited by

    Periodical cited type(13)

    1. 孟向丽,杨淼,黄利平,刘春祥,李旭光. 油井筛管堵塞识别和治理方法. 石油工业技术监督. 2022(04): 7-10 .
    2. 纪成,赵兵,李建斌,罗攀登,房好青. 温度响应地下自生成支撑剂研究. 石油钻探技术. 2022(04): 45-51 . 本站查看
    3. 冯波,柯尊嵩,刘彦广,上官拴通,李翔,崔振鹏. 增强型地热系统储层堵塞机理及解堵技术进展. 天然气工业. 2022(12): 165-183 .
    4. 王巧智,苏延辉,江安,郑春峰,高波,张云飞. 可控冲击波增渗解堵技术实验研究. 天然气与石油. 2021(02): 68-74 .
    5. 张志军,张建文,王世宇,王团. 低渗透油田改性泡沫酸解堵实验分析. 化学工程师. 2021(05): 36-39 .
    6. 周鹏,杜孝友,曹砚锋,于继飞,江海畏,薛启龙. 电爆冲击波增渗解堵技术试验研究. 石油钻探技术. 2020(02): 98-103 . 本站查看
    7. 石洪,郑继龙,陈立群. 渤海J油田氮气泡沫酸化用泡沫酸体系优选. 精细石油化工进展. 2020(01): 10-12+15 .
    8. 肖立晓,侯吉瑞,刘常清,梁拓,赵伟. 醇醚型高效解堵剂的制备与矿场应用. 油田化学. 2020(02): 260-265 .
    9. 高智梁,刘跃忠,张锋利,孟向丽,郝晓军. 渤海Q油田油井筛管堵塞的认识与解堵技术. 石油工业技术监督. 2019(07): 53-54 .
    10. 武文玉. 渤海油田自生泡沫酸化技术研究. 精细石油化工进展. 2019(03): 18-20+33 .
    11. 马靖翔,杨松林,姬华勇,张越,王荫刚. 适用于稠油油藏的新型化学复合解堵技术. 断块油气田. 2019(06): 800-804 .
    12. 孙逢瑞,姚约东,李相方,陈刚,丁冠阳. 基于R-K-S方程的同心双管注多元热流体传热特征研究. 石油钻探技术. 2017(02): 107-114 . 本站查看
    13. 孙逢瑞,姚约东,李相方,孙政,陈刚. 海上非凝结气与过热蒸汽混注井筒传热特征研究. 石油钻探技术. 2017(05): 92-97 . 本站查看

    Other cited types(6)

Catalog

    Article Metrics

    Article views (2525) PDF downloads (2773) Cited by(19)
    Related

    /

    DownLoad:  Full-Size Img  PowerPoint
    Return
    Return